Sunday, December 14, 2025

End of 2025 Update

 

Paradisio, Purgatorio, and Inferno Compressatorio. Get yourselves a cup of your favorite drink and settle in everyone, this is gonna be a long one.

At our last update, 3001 was being wired, 303 was receiving some interior touch ups, and in general life was moving pretty smoothly. Very shortly after that update was published, however, things got a bit more complicated. These have probably been some of the most hectic months in the shop in quite some time, at least in terms of how many cars have been worked on. 

2600 has for a long time had something of a weak compressor. Combine this with the fact that safety cars tend to use a lot of air, and it hasn't been uncommon for the compressor to effectively run almost nonstop for 20 minutes, pause for a few moments, and then kick back on again. It's been something kept on the radar, but never pressing enough to warrant pulling the car from service. Unfortunately, that changed.

While in service towards the end of august it was noted that the air gauge was stubbornly refusing to climb above 50 psi. Any usage of the air that there was wouldn't be made up for unless sitting for an extended period of time. Bringing the car to the shop became something of a harrowing experience as the air dropped so low the doors opened themselves while motoring up the hill. 

2600's compressor rests on mountings that suspend below the car, and support the compressor from below. Generally, a very solid arrangement. However, this does make removing the compressor a bit difficult, as you have to first get the bolts that fasten it out, then lift up on the compressor, move it backwards, lower, twist, and then extract from under the car. There's not a lot of clearance. This also means we need use of the pit, well that's occupied by 3001, which isn't quite to moving itself, and without a roof can't exactly sit outside for any length of time. No matter though, 3001 can be pushed all the way into the shop, loosing us almost all of our working space but oh well, and 2600 can be nosed in enough to get the compressor out, then dragged back out and left outside until the compressor is repaired. That means a lot of equipment has to be moved under not its own power, but oh well, light work for the diesel. 

Enter compressor death number 2. If 2600s compressor refusing to get above 50 psi was bad, the Diesel proved to be much, MUCH worse. It could build to 30, at half throttle, and any reduction and the needles dropped like a stone to barely a tick above 10. Well, there goes the plan to make moves with the diesel. The hero of the day, as it more than often is, came to be line car 1.

Weighing in at, well I don't think anyone really knows, built in 1894, with a body mostly made out of random spare lumber, our Iowan corn fed, all American champion has proven many times to be more than up to the task of dragging around just about anything. The use of LC1 as it turns out is rather fortuitous, but more on that later. 

The Iowan obviously did a fantastic job, and without much fuss at all we had 3001 buried and 2600 nosed into the shop. Removing the compressor took almost all of an afternoon and some of the night, as we were both figuring out how to drop the compressor, but also dealing with a lifting table that was just slightly too tall.

So, what was wrong with 2600's Compressor anyways? Well, a few things, luckily almost all in the head. All of the check valves were rather dirty and covered in gunk. A major smoking gun was found when one of the check valves was found to have snapped in half, blocking the valve from moving at all. This wasn't all though; the head gasket had failed or was failing in multiple places. The gasket itself had been made incorrectly, as holes for the head bolts to pass through had been mis stamped and severely compromised the gasket. It was also mysteriously torn, having lost about half of its width on the lower corner of one of the cylinders. Piston Rings were checked as well, and though still acceptable noted as something that will need replaced in the future. 



Compresor as extracted from under 2600.


Failed Gasket. The missing chunk and bolt holed mis-stamped clearly visible.


Head of the Compressor


A complete, though dirty, example of a Check valve from 2600's compressor.


Snapped in half and failed check, This was one of the major issues that kept the compresor from building air. 


Gratuitous crankcase shot.

A new Gasket was cut, a freshly cleaned up head was put together, with all replacement valves inserted, and the compressor was put back together. Remounting it to the car was far easier, this time knowing the process, but also having now found a lower profile jack to get it under the car in the first place. 2600 was returned to service less than 2 weeks after having to be pulled. 

So, what of the Diesel's compressor? Similarly, a valve issue. upon opening the compressor, a fine copper dust was found to be coating pretty much everything, and one of the intake checks was missing its copper ring seal. Amazingly, a good healthy clean and the valve was able to seal up enough to be put back into service, with plans to order a full head rebuild kit this spring. 

Now, onto Line Car 1. This car has had for a long time a mystery issue that has meant the #2 end controller (west) hasn't been functional. With need for the car to put in some heavy work lugging S193 around for Winterfest setup, it was decided to finally get into the weeds on that controller. The mystery issue that evaded multiple shop departments for years? A single contact finger on the reverse drum was slightly twisted and was not making contact, meaning current couldn't flow through the circuit. 5 minutes with a screw driver, and some light bending against a bench was enough to restore the controller to operation. Well, mostly, the controller itself was still in rough shape, with many elements being heavily worn, some even so far as to have burned into the screws that were holding them to the drum. K10 parts are something that we are fairly thin on, so the controllers are still not perfect, but have been brought to a point where they are safe to run. While undergoing that work, the brake rigging and suspension was all given a greasing. 

Line Car 1 is sadly a car that at the moment lives its life outside, so when the paint on the car was coming off in our hands while working on it, the decision was made to give it a new paint job. The old household paint that had been applied by prior owners came off in big sheets, with no primer under to hold them down. The wood was sanded, new paint and primer was bought, and quickly the car became somehow even more orange than before. Once again, we got the majority of this week done in only a few weeks. LC1 has since put in a good season’s work doing the line car shuffle the length of the line and back, with no issues to report. 



LC1 being Re-Lettered.


Lettering Complete.


Re-Painted for a nice Roster Shot. Since the car came out just at the start of Pumpking Patch Trains,
and is already orange, a plywood Jack-O-Lantern smile was hung from the front.



The Line Car Shuffle begins it's work repairing Chrsitmas light strings.

So, all of that is the saga of the Un-planned work. Now onto some of what we were actually intending to do. 

First of all, an update on 3001. Around the time of the last update, we ran out our stock of wire. Turns out a double end double truck Birney car easily exhaust almost 700 feet of wire, at least for the somewhat more wiring intensive K6 controllers that Conn Co. insisted on using. Ordering the wire took quite some time, but fortunately the wire arrived early November, and the last of the traction cabling has since been run. Motor leads are also all made up, and all the breakouts from the controllers have been tested. Line switch wiring is now complete, as is wiring for the compressor, which has also been plumbed in finally. Though probably the shortest in number of words, as this hasn't been anywhere near the saga of the compressors or LC1, this is actually an incredibly large step forward. This puts us withing arms reach of actually being able to power test the car, and see it take its first steps under its own power in decades. We make no promises on when, as time and resources are all devoted to keeping the fleet running for Winterfest, as well as other general holiday commitments, but it will be soon. 

Moving backwards in time a bit, following the repainting of LC1, and before the arrival of 3001's new wire, a bit of planned work got underway. 303's roof has been bad for some time. If it rains outside, it rains inside. The canvas is heavily deteriorated, possibly never properly treated, and was coated in roofing tar at various points to seal leaks, instead of being fixed correctly. Initially, we'd planned to start on that after 3001's wiring had been completed, which had we not run out of wire would have been in august, leaving us plenty of time to get the roof done for Winterfest. The sudden failure of 2600 and then work on LC1 pushed that work back into October, meaning getting it done in time for Winterfest is no longer an option. Still, with no wire in for 3001, may as well get started anyways. The old Canvas came off fairly easily, the lack of proper treatment and application of tar caused it to become somewhat brittle, so it cracked and came apart with little effort.

Underneath the Canvas, the wood was mostly in good shape, but not perfect. Along both sides holes had been cut to access lighting circuits, and then crudely patched with tin sheeting. Some wood on the vestibule ends was getting quite soft, and along the tail board of the clerestory where the anchor screws had lost most of their purchase. An oddity that was found was in several spots along the car was the addition of several large wooden blocks under the sheathing. These were definitely not original, and some of them were becoming an issue. On both sides of the car, on the west end, the blocking had been placed in such a way that it was raising the sheathing on the main barrel of the roof in such a way that it was no longer in line with the sheathing on the vestibule ends. The gap created had ostensibly been filled with scraps of canvas, but that was most certainly failed and allowing water in. So, a whole section of roof on both sides had to be removed, the blocking removed, and then the sheathing replaced. So what were these blocks for? Well, it's hard to tell. A visit from Randy Hicks confirmed that they were not original to the car’s construction, and were most likely added later on in life. The location of the blocking removed dies potentially offer a clue, as it aligns with the steps and grab irons that one would use to climb the roof. The best guess is that those blocks were there to strengthen the step areas, and were probably installed in the later days of the CA&E at Wheaton Shops. Mis-alignment, rough patching, none of that mattered, this was back then just another long in the tooth car on a road not intending to last very much longer. 



Canvas patching to fill the gap created by missaligned structure.


The added blocking, the added hight above the Carline is very visible. This is the North side of the car, the south side was much worse, with a ap of almost an inch.


The added blocking cleared out. The steel band is part of the cars iriginal structure.


New sheathing in place. 

New canvas has yet to go on the car, and the last bits currently trapped under the poles and running boards has yet to be lifted, a job that will have to wait till next spring. 

Currently, we are focused on getting the fleet through Winterfest. Cold weather often has negative effects on cars, causing tanks to freeze, and ice to creep its way through air systems. Over the doldrums of January and February, 16 is planned to come into the Visitors Center, where it will receive a new coat of paint on its roof, floors, and likely window frames, as well as most likely some more revarnishing. We will also (Hopefully) be finally installing heat back into the car. Working in the VC will give us the chance to work in heat for the first time in years, not only allowing us to do cosmetic works, but also keep up a pace of work that would otherwise be scuppered by the weather.